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HomeMy WebLinkAboutX2015-3751 - SoilsX2015.3751 Vi517 7Zoxburvj R� consultants engineering geotechnical applications CITY OF NEWPORT BEACH March 16, 2017 Building Department Project No. SC883.2 100 Civic Center Drive Newport Beach, CA 92660 Subject: COMPACTION REPORT FOR PLACEMENT OF FILL WITHIN LIMITS OF RESIDENTIAL BUILDING PAD AND SHORING CAISSON BOREHOLES AT 4527 ROXBURY ROAD CORONA DEL MAR, CALIFORNIA City of Newport Beach Permit No.: 2821-2015 References: 1. "Geotechnical Investigation for Proposed Residential Development Located, at 4527 Roxbury Road, Corona Del Mar, California (Cameo Shores), California," by EGA Consultants, LLC, dated July 21, 2015 . 2. "Foundation, Shoring, and Retaining Wall Plans, Fakhimi Residence, 4527 Roxbury Road, Newport Beach, CA," by Core Structure, Inc., dated March 22, 2016. To City Building/Grading Officials: In accordance with the City of Newport Beach building requirements, we are submitting this compaction report for the grading of the subject building pad. This report includes the test results performed at the subject lot during the placement of on-site soil material in the area of the proposed residential building pad. The site earthworks (excavation) operations were performed by the sub -contractor, Don Goodwin, Inc. Conventional grading was not performed as the entire footprint is subterranean basement where over -excavation was not necessary (100% bedrock bottoms). Excavation and grading of the subject lot commenced on October 3, 2016 and was complete by March 14, 2017. The lower basement represents the entire pad which was excavated to the basement slab subgrade. Note: the basement portion of the building pad was created by placing 6 inches of fill over approximately 6 to 14 ft. of cut. The site drainage is gravity -fed to Fairfield Road, and no sump pumps are necessary. Note: due to setbacks of the existing neighboring building adjacent to each side yard boundary, caisson drilling and shoring installation was performed during our continuous observations. The Shoring Plans were provided by Core Structures, Inc. In accordance with the above - referenced Shoring Plan by Core Structures, Inc., on October 17, 2016, through November 23, 2016, a total of fifty-four (54), 29" to 36" diameter caisson boreholes were drilled to total depths of 35 feet to 41 feet below the upper pad elevation. The drilling sub -contractor was Leon Krous Drilling, Inc., employing a SR30 drill rig crane. Representatives from our firm inspected and confirmed that each of the fifty-four boreholes extend into competent native materials. The caisson embedments meet or exceed the specifications outlined by Core Structures, Inc. in the Site Shoring Plan. The drilled Pier Schedule is presented as Table 3, herein. Also, see a copy of the Caisson Layout Plan, attached. 375-C Monte Vista Avenue - Costa Mesa, CA 92627 - (949) 642-9309 • FAX (949) 642-1290 Prior to the placement of fill, the excavation bottoms were inspected and approved by a Certified Engineering Geologist employed by EGA Consultants. The exposed surface was scarified, moisture conditioned and recompacted to a minimum of 90% relative compaction. Field density test results are tabulated on Table 1, Summary of Field Density Tests. One Caterpillar 973 front loader and one Caterpillar 289 tractor were utilized for the purpose of compaction and grading control. Water was added via a 2 -inch fire hose and moisture contents were at near -optimum moisture levels. All earthwork operations were performed under continuous observations by this firm and were performed in accordance with geotechnical specifications outlined in the referenced soils report dated July 21, 2016. The building pad was graded in accordance with the 2013 CBC and the City of Newport Beach Building standards and are approved for construction. Based on our continuous observations and testing, the subject and adjacent sites are not impacted by the site grading operations to date. This report includes the test results performed at the subject site during the placement of on- site and imported soil material in the area of the proposed building pad. Additional observations and testing are required in areas to receive exterior improvements (driveway approach, patio flatwork, drainage, etc.) and utility trench backfill. I certify that all rough grading work was done in compliance with the above -referenced soils report and the work complies with City of Newport Beach grading regulations. All soils values and geotechnical specifications outlined in the Soils Report remain valid. This opportunity to be of service is appreciated. If you have any questions, please call. Very truly yours, EGA Consultants, LLC DAVID A. WORTHINGTON CEG 2124 Principal Engineering Geologist Copies: (2) Addressee (1) SC Homes, Inc. Ann: Jeremy Rogers PAD CERTIFICATION REPORT: 4527 Roxbury Rd., Newport Beach (CDM), CA Project No. SC883.2 March 16, 2017 `` pavid A• �orth►n�°n � N°•c PG2E � �a ENGINET-a TABLE 1 SUMMARY OF MOISTURE DENSITY RELATIONSHIPS (ASTM: D1556) "FG" = Finish Grade (Ground Level Pad). Note: the Basement Pad was created by scarifying the bottom 6 inches and re -compacting to the basement slab subgrade elevation. TABLE 2 SUMMARY OF MAXIMUM DENSITY TEST (ASTM D 1557) Sample FE:::]Location pth Dry Moisture Maximum Optimum Relative low Density Content Density Moisture Compaction ISWCBasement d ft PCF % PCF °/, G 113.0 12.5 120.5 11.5 94 FD -2 FG 112.1 12.0 120.5 11.5 93 NWC Basement Basement FD -3 FG 115.7 13.1 120.5 11.5 96 Central Basement Basement FD -4 FG 114.8 13.0 120.5 11.5 95 Garage Basement Basement FD -5 FG 115.8 12.6 120.5 11.5 96 SWC Basement Basement "FG" = Finish Grade (Ground Level Pad). Note: the Basement Pad was created by scarifying the bottom 6 inches and re -compacting to the basement slab subgrade elevation. TABLE 2 SUMMARY OF MAXIMUM DENSITY TEST (ASTM D 1557) Sample FE:::]Location Maximum Density Optimum Moisture Pcffol Fill (per Soils Report dated 7/21/16) 120.5 11.5 PAD CERTIFICATION REPORT: 4527 Roxbury Rd., Newport Beach (COM), CA Project No. SC886.2 March 16, 2017 TABLE 3 SUMMARY OF CAISSON EXCAVATION OBSERVATIONS Caisson/Pile Number SP -1 Date Completed 10/31/2016 Caisson/Pile Diameter 32" Total Depth below pad elev. 41.0 ft. SP -2 11/1/2016 32" 35.0 ft. SP -3 11/2/2016 32" 36.0 ft. SP -4 11/3/2016 36" 40.0 ft. SP -5 11/2/2016 36" 40.0 ft. SP -6 11/3/2016 36" 40.0 ft. SP -7 11/2/2016 36" 40.0 ft. SP -8 11/9/2016 36" 40.0 ft. SP -9 10/17/2016 32" 36.0 ft. SP -10 10/20/2016 32" 35.0 ft. SP -11 10/17/2016 32" 36.0 ft SP -12 10/20/2016 32' 36.0 ft. SP -13 10/17/2016 32" 36.0 ft SP -14 11/3/2016 32" 36.0 ft SP -15 11/9/2016 32" 35.0 ft SP -16 10/17/2016 32" 36.0 ft SP -17 11/19/2016 36" 41.0 ft. SP -18 11/9/2016 36" 40.0 ft. SP -19 11/19/2016 36" 40.0 ft. SP -20 11/8/2016 36" 40.0 ft. SP -21 11/15/2016 36" 40.0 ft. SP -22 10/19/2016 32" 35.0 ft. SP -23 10/28/2016 32" 35.0 ft. SP -24 10/31/2016 32" 35.0 ft. SP -25 10/25/2016 32" 35.0 ft. SP -26 11/7/2016 36" 40.0 ft. PAD CERTIFICATION REPORT: 4527 Roxbury Rd., Newport Beach (CDM), CA Project No. SC663.2 March 16, 2017 PAD CERTIFICATION REPORT: 4527 Roxbury Rd., Newport Beach (CDM), CA Project No. SC883.2 March 16, 2017 Caisson/Pile Number Date Completed Caisson/Pile Diameter Total Depth below ad elev. SP-27 11/21/2016 36" 40.0 ft. SP-28 11/22/2016 36" 40.0 ft. SP-29 11/11/2016 36" 40.0 ft. SP-30 11/21/2016 36" 40.0 ft. SP-31 11/4/2016 36" 40.0 ft. SP-32 10/25/2016 36" 40.0 ft. SP-33 10/18/2016 32" 35.0 ft. SP-34 10/26/2016 32" 35.0 ft. SP-35 10/31/2016 32" 35.0 ft. SP-36 10/26/2016 32" 35.5 ft. SP-37 10/28/2016 32" 35.0 ft. SP-38 11/1/2016 32" 35.0 ft. SP-39 10/26/2016 32" 35.0 ft. SP-40 10/27/2016 32" 35.0 ft. SP-41 10/26/2016 32" 36.0 ft. SP-42 11/1/2016 32" 35.0 ft. SP-43 10/25/2016 32" 35.0 ft. SP-44 10/31/2016 32" 35.0 ft. SP-45 11/4/2016 36" 40.0 ft. SP-46 11/8/2016 36" 40.0 ft. SP-47 11/23/2016 36" 40.0 ft. SP-48 11/22/2016 36" 40.0 ft. SP-49 11/23/2016 36" 40.0 ft. SP-50 11/22/2015 32" 37.0 ft. SP-51 11/11/2016 29" 36.0 ft. SP-52 11/18/2016 29" 35.0 ft. SP 53 10/28/2016 29" 35.0 ft. SP-54 10/19/2016 29" 35.0 ft. PAD CERTIFICATION REPORT: 4527 Roxbury Rd., Newport Beach (CDM), CA Project No. SC883.2 March 16, 2017 V NOTE: Each caisson excavation extends a minimum of 25 feet into competent bedrock. All caisson excavation bottoms were inspected and noted to be free of loose debris and pre - moistened prior to steel placement and concrete pour. Excavations, caisson drilling, lagging, and preparations were performed in accordance with the referenced soils report by EGA Consultants, and Shoring Plan by Core Structures, Inc.. The annulus spaces behind the timber lagging was backfilled by a combination of spoils compacted via pogo mechanical wacker coupled with 2 -sack slurry via a 2 -hose accessed through cut porthole slots. Backfill was performed during our oversight, observations and documentation. PAD CERTIFICATION REPORT: 4527 Roxbury Rd., Newport Beach (CDM), CA Project No. SC883.2 March 18, 2017 6 ®engineering � geotechnical applications consultants CITY OF NEWPORT BEACH May 24, 2019 Building Department Project No. SC883.3 100 Civic Center Drive Newport Beach, CA 92660 Subject: FINAL GRADING CERTIFICATE HARDSCAPE COMPACTION, UTILITY TRENCH and RETAINING WALL BACKFILL at NEW RESIDENTIAL PROPERTY LOCATED AT 4527 ROXBURY ROAD CORONA DEL MAR, CALIFORNIA City of Newport Beach Permit No.: 2821-2015 References: 1. "Geotechnical Investigation for Proposed Residential Development Located, at 4527 Roxbury Road, Corona Del Mar, California (Cameo Shores), California," by EGA Consultants, dated July 21, 2015. 2. "Foundation, Shoring, and Retaining Wall Plans, Fakhimi Residence, 4527 Roxbury Road, Newport Beach, CA," by Core Structure, Inc., dated March 22, 2016. To City Building/Grading Officials: In accordance with the City of Newport Beach building and grading requirements, we are submitting this final compaction report for the temporary shoring drilling/installation, grading of the full basement building pad, utility trench backfill, retaining walls backfill, and exterior improvements. This report covers both the upper exterior grade and the lower basement pad (with approach, multiple planter boxes and retaining walls). Conventional grading was performed only for the upper building pad, as the entire lower footprint is subterranean basement where over -excavation was not necessary (100% bedrock bottoms to be overlain by a layer of crushed rock for the sub -mat slab blanket drainage). The site earthworks operations were performed by the sub -contractors, Don Goodwin, Inc. Excavation and grading of the subject lot commenced on October 3, 2016 and was completed on March 14, 2017. The retaining/basement wall backfill, pool/spa prep and hardscape was completed by May 23, 2019. The lower basement represents the entire pad which was excavated to the basement slab subgrade. Note: the basement portion of the building pad was created by placing 6 inches of fill over approximately 6 to 14 ft. of cut. The site drainage is gravity -fed to Fairfield Road, and no sump pumps are necessary. Due to setbacks of the existing neighboring building adjacent to each side yard boundary, caisson drilling and shoring installation was performed during our continuous observations. The Shoring Plans were provided by Core Structures, Inc. and approved by the City of Newport Beach Building Department (see referenced 2, above). In accordance with the above -referenced Shoring Plan by Core Structures, Inc., on October 17, 2016, through November 23, 2016, a total of fifty-four (54), 29" to 36" diameter caisson boreholes were drilled to total depths of 35 feet to 41 feet below the upper pad elevation. The drilling sub- contractor was Leon Krous Drilling, Inc., employing a SR30 drill rig crane. Representatives from our firm inspected and confirmed that each of the fifty-four boreholes extend into competent native materials. The caisson embedments meet or exceed the specifications outlined by Core Structures, Inc. in the Site Shoring Plan. The drilled Pier Schedule is presented as Table 3, herein. Prior to the placement of fill, the excavation bottoms were inspected and approved by a Certified Engineering Geologist employed by EGA Consultants. The exposed surface was scarified, moisture conditioned and recompacted to a minimum of 90% relative compaction. Field density test results are tabulated on Table 1, Summary of Field Density Tests. 375.-C Monte Vista Avenue • Costa Mesa, CA 92627 • (949) 642-9309 • FAX (949) 642-1290 One Caterpillar 973 front loader, one Caterpillar 289 tractor, one Caterpillar 308E mini -excavator, coupled with wackers/vibratory plates were utilized for the purpose of compaction and grading control. Water was extensively added via a 2 -inch fire hose and moisture contents were at near -optimum moisture levels. All earthwork operations were performed under continuous observations by this firm and were performed in accordance with geotechnical specifications outlined in the soils report dated July 21, 2015. For all site retaining/subterranean walls, we have observed the installation of the min. 4 -inch dia. PVC retaining wall back -drain pipes (SDR 35 or equiv.) backfilled with %-inch crushed rock wrapped in filter fabric ("geofabric"). The PVC pipes were placed with perforations -down, length -wise along the flowlines behind the new retaining walls. The new subterranean backdrains are tight -lined via solid pipes (min. fl- inch dia.),which gravity -discharge to the cored curbface at Fairfield Drive. Additionally, prior to the placement of %-inch gravel backfill in the lower H/3 of the wall backfill, the excavation bottoms were inspected and approved by a representative of the Certified Engineering Geologist employed by EGA Consultants. All basement/retaining wall backfill was inspected/tested/documented and approved by a qualified representative of EGA Consultants. Spoils used as backfill above the filter fabric were compacted to a minimum of 90% relative compaction. The backdrains and backfill were approved and are suitable for the intended use from a geotechnical standpoint I certify that all shoring, grading and compaction work was done in compliance with the soils report for this project and the work complies with City of Newport Beach grading regulations. All soils values and geotechnical specifications outlined in the soils report remain valid. Based on our continuous observations and testing, the subject and adjacent sites are not impacted by the site grading operations. This opportunity to be of service is appreciated. If you have any questions, please call Very truly yours, EGA Consultants, Inc. ��EFIED Q Wormli7gta DAVID A. WORTHINGTON CEG 2124 )f No, CECpyzq Principal Engineering Geologist CER Eb /I2 N-� ENGINEERIN�t 46. GEOCOG(ST Copies: (2) Addressee (1) SC Homes, Attn: Jeremy Rogers o Q l'' ��ALtF% FINAL COMPACTION REPORT: 4527 Roxbury Road, Corona Del Mar, CA Project No. SC883.3 May 24, 2019 TABLE 1 SUMMARY OF MOISTURE DENSITY RELATIONSHIPS (ASTM: D1556) Sample Depth, -Dry Moisture Maximum Optimum Relative Number/ Below Density Content Density Moisture Compaction Location Pad ft PCF % PCF FD -1 FG 113.0 12.5 120.5 11.5 94 SWC Basement Basement FD -2 FG 112.1 12.0 120.5 11.5 93 NWC Basement Basement FD -3 FG 115.7 13.1 120.5 11.5 96 Central Basement Basement FD -4 FG 114.8 13.0 120.5 11.5 95 Garage Basement Basement FD -5 FG 115.8 12.6 120.5 11.5 96 SWC Basement Basement FD -6 6.0 108.8 13.0 120.5 11.5 90 Retaining Wall Backfill FD -7 4.0 111.8 12.4 120.5 11.5 93 Retaining Wall Backfill FD -8 2.5 110.9 12.1 120.5 11.5 92 Retaining Wall Backfill FD -9 5.5 110.1 13.5 120.5 11.5 91 Retaining Wall Backfill FD -10 4.0 111.7 12.0 120.5 11.5 93 Retaining Wall Backfill FD -11 2.5 111.1 12.7 120.5 11.5 92 Retaining Wall Backfill FD -12 1.5 114.0 12.5 120.5 11.5 95 Retaining Wall Backfill FD -13 3.5 109.5 13.0 120.5 11.5 91 Retaining Wall Backfill FINAL COMPACTION REPORT: 4527 Roxbury Road, Corona Del Mar, CA Project No. SC883.3 May 24, 2019 FD -14 2.0 112.8 11.5 120.5 11.5 94 Retaining SP -2 Fill (per Soils Report dated July 21, 2015) 120.5 11.5 SP -3 11/2/2016 Wall Backfill 36.0 ft. SP -4 11/3/2016 36" 40.0 ft. SP -5 FD -15 2.0 113.6 12.0 120.5 11.5 94 Retaining Wall Backfill FD -16 1.0 108.7 13.5 120.5 11.5 90 Util Trench Backfill FD -17 FG 109.9 13.1 120.5 11.5 91 Util Trench Backfill FD -18 FG 114.9 11.4 120.5 11.5 95 Hardscape FD -19 FG 117.0 11.5 120.5 11.5 97 Approach FD -20 FG 113.6 11.4 120.5 11.5 94 Hardscape "FG" = Finish Grade (Ground Level Pad). Note: the Basement Pad was created by scarifying the bottom 6 inches and re -compacting to the basement slab subgrade elevation. TABLE 2 SUMMARY OF MAXIMUM DENSITY TEST (ASTM D 1557) Sample Maximum Optimum Location Density Moisture 32" Pof SP -2 Fill (per Soils Report dated July 21, 2015) 120.5 11.5 TABLE 3 SUMMARY OF CAISSON EXCAVATION OBSERVATIONS Caisson/Pile Number Date Completed Caisson/Pile Diameter Total Depth below pad elev. SP -1 10/31/2016 32" 41.0 ft. SP -2 11/1/2016 32" 35.0 ft. SP -3 11/2/2016 32" 36.0 ft. SP -4 11/3/2016 36" 40.0 ft. SP -5 11/2/2016 36" 40.0 ft. FINAL COMPACTION REPORT: 4527 Roxbury Road, Corona Del Mar, CA Project No. SC883.3 May 24, 2019 Caisson/Pile NumberCompleted Date Caisson/Pile Diameter Total Depth below pad elev.) SP -6 11/3/2016 36" 40.0 ft. SP -7 11/2/2016 36" 40.0 ft. SP -8 11/9/2016 36" 40.0 ft. SP -9 10/17/2016 32" 36.0 ft. SP -10 10/20/2016 32" 35.0 ft. SP -11 10/17/2016 32" 36.0 ft SP -12 10/20/2016 32" 36.0 ft. SP -13 10/17/2016 32" 36.0 ft SP -14 11/3/2016 32" 36.0 ft SP -15 11/9/2016 32" 35.0 ft SP -16 10/17/2016 32" 36.0 ft SP -17 11/19/2016 36" 41.0 ft. SP -18 11/9/2016 36" 40.0 ft. SP -19 11/19/2016 36" 40.0 ft. SP -20 11/8/2016 36" 40.0 ft. SP -21 11/15/2016 36" 40.0 ft. SP -22 10/19/2016 32" 35.0 ft. SP -23 10/28/2016 32" 35.0 ft. SP -24 10/31/2016 32" 35.0 ft. SP -25 10/25/2016 32" 35.0 ft. SP -26 11/7/2016 36" 40.0 ft. SP -27 11/21/2016 36" 40.0 ft. SP -28 11/22/2016 36" 40.0 ft. SP -29 11/11/2016 36" 40.0 ft. SP -30 11/21/2016 36" 40.0 ft. SP -31 11/4/2016 36" 40.0 ft. SP -32 10/25/2016 36" 40.0 ft. SP -33 10/18/2016 32" 35.0 ft. FINAL COMPACTION REPORT: 4527 Roxbury Road, Corona Del Mar, CA Project No. SC883.3 May 24, 2019 Caisson/PileDate Number Completed Caisson/Pile Diameter Total Depth below pad elev. SP -34 10/26/2016 32" 35.0 ft. SP -35 10/31/2016 32" 35.0 ft. SP -36 10/26/2016 32" 35.5 ft. SP -37 10/28/2016 32" 35.0 ft. SP -38 11/1/2016 32" 35.0 ft. SP -39 10/26/2016 32" 35.0 ft. SP -40 10/27/2016 32" 35.0 ft. SP -41 10/26/2016 32" 36.0 ft. SP -42 11/1/2016 32" 35.0 ft. SP -43 10/25/2016 32" 35.0 ft. SP -44 10/31/2016 32" 35.0 ft. SP -45 11/4/2016 36" 40.0 ft. SP -46 11/8/2016 36" 40.0 ft. SP -47 11/23/2016 36" 40.0 ft. SP -48 11/22/2016 36" 40.0 ft. SP -49 11/23/2016 36" 40.0 ft. SP -50 11/22/2016 32" 37.0 ft. SP -51 11/11/2016 29" 36.0 ft. SP -52 11/18/2016 29" 35.0 ft. SP -53 10/28/2016 29" 35.0 ft. SP -54 10/19/2016 29" 35.0 ft. NOTE., Each caisson excavation extends a minimum of 25 feet into competent bedrock. All caisson excavation bottoms were inspected and noted to be free of loose debris and pre -moistened prior to steel placement and concrete pour. Excavations, caisson drilling, lagging, and preparations were performed in accordance with the referenced soils report by EGA Consultants, and Shoring Plan by Core Structures, Inc.. The annulus spaces behind the timber lagging was backfilled by a combination of spoils compacted via pogo mechanical wacker coupled with 2 -sack slurry via a 2 -hose accessed through cut porthole slots. Backfill was performed during our oversight, observations and documentation. FINAL COMPACTION REPORT: 4527 Roxbury Road, Corona Del Mar, CA Project No. SC883.3 May 24, 2019